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DL was cold bent several degrees. Perhaps I could have accommodated the necessary angle simply by filing the root of the lug bore, I've done it that way before to a smaller angle change, but I bent this one. The flanks of the DT spigot opened up considerably. With the solid bending bars in the lug, the HT bar in the vise, I used a small diameter drift, maybe 1/4" OD with a slightly rounded head, and hundreds of light hammer taps to slowly shrink the spigot flanks down to the new tube location; not just the shoreline but through the whole length. Lots of work and trial & error but I eventually got a pretty decent fit. Same thing for the CS sockets though I bent them hot, and with cups threaded in. The inside half of the spigots needed a lot of movement and shrinking to fit properly and provide the necessary tire clearance. Those fit up well enough to wick filler well, the DL fit better, though there is always room for improvement. I have a better, but still rudimentary, grasp of this sort of procedure. With practice I think one could get reasonably quick & efficient at several degrees of angle change, ending up with spigots having optimum clearance. It was pretty satisfying and I'm looking forward to getting better at this....and not missing any areas! Where the lugs fit well the filler flow was easy and the shorelines took care of themselves.
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